Pilots rescued after Boeing 737 cargo plane makes emergency landing off Hawaii coast, FAA says
Source: USA Today
N'dea Yancey-Bragg USA TODAY
Published 11:14 am ET July 2, 2021/ Updated 4:09 pm July 2, 2021
A Boeing 737-200 cargo plane with two people aboard made an emergency landing in the water off the coast of Hawaii on Friday morning, according to the Federal Aviation Administration.
The pilots of Transair Flight 810 reported engine trouble and attempted to return to Honolulu before they decided to land the plane in the ocean, officials said in a statement.
The pilots, who were en route to Maui, reported one engine was down and then lost their second engine before 2 a.m., ABC News reported citing the state's department of transportation.
Read more: https://www.usatoday.com/story/news/nation/2021/07/02/boeing-737-cargo-plane-emergency-landing-off-hawaii/7839679002/
Mysterian
(4,587 posts)I hope they both recover quickly.
raccoon
(31,110 posts)that was a much older 737 from the 1970s
trof
(54,256 posts)The 200 model is a workhorse.
Wonder if there was fuel contamination. Double engine failure is very rare.
Warpy
(111,261 posts)especially since it's happened before, don't remember the details.
Bo Zarts
(25,397 posts)I flew the 737-200s for a while. Low-tech, like me. Fuel contamination, fuel starvation, multiple bird strikes all come to mind.
turbinetree
(24,701 posts)it has JT8D Low by-pass engines, great AC to work on, because the engines were low..., so the plane sat low compared to the high by pass engines that you see today...around 10, 000 have been built...
HUAJIAO
(2,385 posts)many were fitted with "mud flaps' behind the landing gear as they were used a lot on unimproved landing strips.... much smaller engines nacelles than the 737s we are used to seeing...
Major Nikon
(36,827 posts)The plane would have flown just fine with one engine. Perhaps some contaminates which clogged one side and inevitably shut down the other.
iluvtennis
(19,858 posts)James48
(4,436 posts)They never got above 2500 feet, and began losing altitude the moment the first engine quit/ or was shut down. Unable to climb on one.
So either fuel problems were possible, or an overloaded airplane that couldnt climb with one engine out.
Video of communications feed:
Here is the flight data- he was only in the air for 12 minutes. The Coast Guard found the wreckage and the two victims an hour after the crash. https://flightaware.com/live/flight/RDS810/history/20210702/1100Z/PHNL/PHOG/tracklog
Scruffy1
(3,256 posts)If your having a bad day think of losing your other motor and having to ditch. As an aside, having no knowledge of what caused this nightmare, I remember a conversation about cargo hauling with a former major airline mechanic. He said: " You can always get some to sign off on it."
at 1am into the Pacific Ocean. Someone had a bad day.
I wonder did the lose both engines or too much height while turning to get back to the airfield?
jmowreader
(50,557 posts)the first engine died for whatever reason, and the other one overheated. The flight commenced in the 1AM hour, so outside air temperature shouldn't have been a factor.
The airline has been in operation since 1982 and this was their first incident, so they seem to be a good operator.
Rollo
(2,559 posts)Hope the pilots make full recoveries. They may be lucky to be alive.
It also may take a while before the cause(s) of the multiple engine failures is/are known.
Also, all existing 737's of that vintage probably could use additional inspections.
EX500rider
(10,848 posts)Saw this over at the airliners.net forum:
The utilization of that airframe (N810TA) has been crazy. 60+ cycles in the past week alone on an bird that's 46 years old.
&
she had 71,706 hours and 67194 cycles.
&
Would be very, very unlikely that a fuel issue, as some have speculated regarding potential cause, (were talking PHNL here, a very large airport) had anything to do with this event. PHNL departures are ongoing.
Maybe bird strike or they shut down the wrong engine or bad fuel.
mn9driver
(4,425 posts)Maintenance records for that aircraft, is that the right engine had been written up at least twice recently for high EGT on takeoff. Aside from signing off the discrepancy as noted, there doesnt appear to have been any actual fix applied.
If this turns out to be accurate, the operating certificate for the airline will probably be suspended until they can demonstrate their maintenance problems have been addressed.